Flight No.: 3-64-95 Scheduled Date: October 17, 1967
Pilot: Major Wm. J. Knight
Purpose: 1. Ames Boost Guidance (14) - Burke
2. Solar Spectrum Measurement (29) - BryantLaunch: Smith Ranch #1 on a magnetic heading of 170°3. Ultraviolet Plume (3c) - Bryant
4. Micrometeorite Collector (13) - Bryant
5. Tip Pod Camera (42a) - Bryant
MH-96 "Adaptive," Reaction Controls "Auto," BCS "ON," BG/b engaged, acom = 11°, PAI switch to "Heading," Ventral OFF.
Launch point coordinates: 39° 29.5' N, 117° 11.5' W.
Instrumentation
Engineer: R. Borek
No. | Time | Alt | V | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine at 100%T. Rotate at a = 11° until q = 37°. Fly BG null until burnout. (q = 37° will be flown if BG malfunctions.) Engage "roll-hold" after establishing 0° heading error. |
2. | 25 | 52 | 1650 | 11 | 450 | q = 37°. Maintain q = 37° until burnout. |
3. | 84.4 | 150 | 5595 | 8 | 56 | Burnout. (If burnout has not occurred, shutdown at 5700 fps.) Switch to PAI. Pushover to, and maintain a = 0°. Roll A/C ±10° at less than 5°/sec. Switch to PAI. Engine Master OFF. |
4. | 91 | 170 | 5500 | 0 | 26 | Micrometeorite switch to EXTEND. JPL experiment switch to ON. |
5. | 121 | 230 | 5150 | 0 | 3 | Switch to comp. a. |
6. | 176 | 273 | 4890 | 0 | .2 | Peak altitude. Maintain q, F, & Y within ±2° until a = 22°. |
7. | 231 | 230 | 5150 | 18 | 3 | Switch to Ball Nose a. |
8. | 241 | 210 | 5200 | 22 | 6 | a = 22°. Maintain a = 22° until An = 5g. Switch to a/b. Roll-hold OFF. (Qmax » 850 psf). Micrometeorite to "RETRACT." JPL switch to OFF. Pod camera switch to ON. |
9. | 292 | 95 | 5050 | 22 | 525 | An = 5.0g. Maintain 5g until H dot = -400 fps. |
10. | 304 | 82 | 4350 | 17 | 710 | H dot = -400 fps. Pushover to maintain H = 80K ft until 50 N. M. |
11. | 320 | 80 | 4000 | 4 | 695 | 50 N.M. Extend speed brakes to 20°. Start right turn to » 180°. Pushover to obtain H dot = -300 fps. |
12. | 365 | 70 | 3000 | 4 | 600 | Cuddeback. Increase H dot to -400 fps. Vector to Hi-Key. Speed brakes as required. |
13. | High Key - Check flap and "squat" circuit breakers in. Arm stick kicker and third skid. Engine Master "OFF." (2) Radiometer switches OFF. Window Shade Down. |
NOTES:
2. Emergency lakes: Mud, Ballarat, Cuddeback.
3. Flight duration: Approximately 12 minutes.
4. Flight plan based on 60,000lb thrust at 100%. Engine #103.
Total burn time at 100% T. (60,000lb) = 84.4 seconds.
Launch wt = 33,818lb Burnout wt = 15,341lb
c.g = c.g. =
5. Ground jettison check (Accounted for in wts. and burn time).
6. Precision attitudes preset: Pitch = 0.0 (90.0)
Roll = 0.0 (90.0)
Heading = 170°
2. FCS malfunction as indicated on analyzer check list.
3. Malfunction of inertial platform.
4. Malfunction of ball nose.
5. Malfunction of either BCS.
6. Malfunction of
precision heading.
Failure | Action | ||
1. | Radio or radar | 1. | Proceed as planned. |
2. | ANY damper failure or failure to fixed gain | 2a. | 0
- 35 seconds
Switch to a/b. Fly q = 30° in place of q = 37°. Pushover to a = 2° at 35 sec. Proceed to burnout. (Hmax = 135K, V = 5910.) Fly a = 15° to H dot = -200 fps. Then fly H dot = -200 fps to 50 N.M. (H = 85K, V = 3900) |
2b. | 35
sec. - Burnout
Switch to a/b. Pushover to a = 2° when failure occurs. Proceed to burnout. If reentry is required, use a = 15° to H = 250K. Above 250K, use a = 17°. |
||
2c. | After
Burnout
Use a = 17° for reentry. |
||
3. | Ball Nose Failure | 3a. | 0
- 35 seconds
Switch to comp. a. Pushover to 0g at 35 seconds. Proceed to burnout. (Hmax = 125K, V=5865). Fly H dot = -250 fps to 50 N.M. (H = 81K, V = 3700 fps.) |
3b. | 35
sec. - Burnout
Switch to comp. a. Pushover to 0g when failure occurs. Proceed to burnout. If reentry is required, use q = 0° to 220K, q = -5° to 250K, and q = -10° above 250K. (dHmax = -25°.) |
||
3c. | After
Burnout
Switch to comp. a. Use q = -10° for reentry. (dHmax = -25°.) |
||
4. | Attitude Failure | 4. | Use a = 5° in place of q = 37° at 25 sec. Switch to a/b. Proceed with 3a, b, or c as applicable. (Use a for reentry, if a reentry is required.) |
5. | Inertial Failure | 5. | Switch to a/b. Proceed as planned. |
6. | Delayed Light | 6. | Rotate to 2.5g. Proceed as planned. |
7. | Boost Guidance | 7. | Fly q = 37° in place of BG null at 25 sec. Proceed as planned. |
INADVERTENT ENGINE SHUTDOWN:
0 - 43 sec Smith Ranch
43 - 68 sec Mud Lake (2500 fps)
68 - 73.5 sec Ballarat (4100 fps)
73.5 - 76 sec Cuddeback (4600 fps)
76 - Up sec Edwards
(4800 fps)
Approved
E. J. Adkins, Head X-15 Project Office