Flight No.: 3-44-67 Scheduled Date: June 29, 1965
Pilot: Capt. Joe Engle
Purpose: To obtain
data for the following programs:
1. LRC Scanner, NSL Radiometer - (Joe Lapierre)2. BLN - (Tom Lewis)
3. Reentry Maneuver Techniques
Instrumentation
Engineer - Febo Bartoli
Launch: Delamar Lake on magnetic heading of 215° , MH-96 Adaptive, R.C. "AUTO", B.C.S. "ON", heading vernier "STANDBY"
Launch Point Coordinates:
114°
35Æ W, 37°
22ÆN.
No. | Time | Alt | V | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine, increase to 100% T, rotate to a» 11° , maintain a» 11° to q =42° . |
2. | 32 | 56 | 2000 | 11 | 550 | q= 42° , maintain q =42° |
3. | 82 | 147 | 5100 | 7 | 420 | Shutdown at 5100 fps, pushover to a»0° |
4. | 104 | 200 | 4650 | 0 | 4 | Check b=0 , heading vernier to "DY " |
5. | 139 | 260 | 4350 | 0 | .4 | Roll manuever ±5° . |
6. | 175 | 283 | 4150 | 0 | .25 | Peak altitude, extend speed brakes to 20°. |
7. | 200 | 240 | 4200 | 0 | .5 | q = -12, maintain q = -12 to a = 23°. |
8. | 246 | 200 | 4700 | 17 | 4 | Heading vernier to "STANDBY." |
9. | 261 | 165 | 5000 | 23 | 25 | a = 23°, maintain a = 23° to g max = 5, max reentry q » 1150 psf. |
10. | 285 | 100 | 5000 | 20 | 400 | H dot = -800, pushover to maintain -500, extend speed brakes to -35°, R.C. "OFF." |
11. | 310 | 60 | 3600 | 4 | 1400 | Cuddeback, vector to high key, speed brakes as required. |
12. | High Key - check flap and "Squat" circuit breakers in. Data calibrate, experiment switch "OFF." | |||||
Before APU shutdown, cycle flaps, set stabilizer trim to zero, data "Off." |
Notes:
2. Emergency lakes: Hidden Hills and Cuddeback.
3. Flight duration: Approximately 12 minutes.
4. Flight plan based on 58,750lb thrust - Engine (#107).
Total burn time at 100% = 83 sec.
Launch Wt. = 33,700lb
Burnout Wt. = 15,550lb
2. Malfunction of inertial platform.
3. Malfunction of ball nose.
4. Radio, radar
or T.M. malfunction.
Failure | Action | ||
1. | Radio or Radar | Proceed as planned. | |
2. | Total
damper any axis,
failure to fixed gain any axis (For roll failure turn yaw off) |
(a) | 0
- 32 sec.
Alternate Flight Plan. Proceed normally until t = 32 sec. At 32 sec. pushover to » 2° a and extend speed brakes to 35°. Shutdown at 5200 fps and retract speed brakes to 20° after shutdown. Vector to high key (q » 550 psf). Peak altitude » 145,000 ft. |
(b) | Attitude | (b) | Hold 11° a till t = 32 sec, then proceed with alternate flight plan. |
(c) | Ball Nose | (c) | Same as alternate, except use » 0.1 g instead of 2° a. Heading vernier to "·Y." |
3. | Total
damper any axis,
failure to fixed gain any axis (For roll failure turn yaw off) |
(a) | 32
sec - S.D.
Pushover to 2° a and extend speed brakes when failure occurs. Shutdown at 5200 fps. Reenter at 20° a and 20° speed brakes. |
(b) | Attitude | (b) | Same as 3 (a). |
(c) | Ball Nose | (c) | Same as 3 (a) except use » 0.1 g instead of 2° a. Use q = 0 for reentry. |
4. | Total
damper any axis,
failure to fixed gain any axis (For roll failure turn yaw off) |
(a) | After
Shutdown
Proceed as planned, reenter at 20° a. |
(b) | Attitude | (b) | Proceed as planned. |
(c) | Ball Nose | (c) | Use q = -10° for reentry. |
5. | Delayed engine light | Proceed - shut down at 5000 fps. |
6. Inadvertent engine shutdown:
0 - 42 sec Delamar
42 - 44 sec
44 - 68 sec Hidden Hills (2555 fps)
68 - 72 sec Cuddeback (3900 fps)
72 - Up sec Edwards (4200 fps)