Flight No.: 3-43-66 Scheduled Date: June 15, 1965
Pilot: Capt. Joe Engle
Purpose: To obtain
data for the following programs:
1. NSL Radiometer - (Joe Lapierre)2. Boundary layer noise - (Tom Lewis)
Instrumentation
Engineer: Febo Bartoli
Launch: Delamar Lake #1 on a magnetic heading of 215°, MH-96 Adaptive, R.C. "AUTO," BCS "ON," heading vernier to "Standby," ventral off.
Launch point coordinates:
37° 18' N, 114° 36' W.
No. | Time | Alt | V | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine, increase to 100%T. Rotate at a = at 11° (» 2g) until q = 38°. |
2. | 28 | 52 | 1800 | 11 | 540 | q = 38°. Maintain q = 38°. |
3. | 79 | 135 | 5000 | 8 | 87 | Shutdown. Check b = 0, switch heading vernier to "·Y." Maintain a » 0°. |
4. | 161 | 240 | 4200 | 0 | 3 | Peak altitude. Maintain q = 0 until a = 23°. Extend speed brakes to 20°. Heading vernier to "STANDBY." |
5. | 225 | 175 | 4650 | 23 | 17 | a = 23°. Maintain a = 23° until H dot » -800 fps. (Max reentry g » 4.5). Extend speed brakes to 35°. |
6. | 260 | 96 | 4600 | 4 | 410 | H dot » -800 fps, reduce a to maintain H dot » -400 fps. Maintain q constant » 700 psf. |
7. | 300 | 63 | 3000 | 4 | 900 | Cuddeback - Vector to High Key, speed brakes as required. |
8. | High Key - check flap and "Squat" circuit breakers in. Data calibrate, experiment #1 "OFF." | |||||
Before APU shutdown, cycle flaps, set stabilizer trim to zero, data "Off." |
Notes:
2. Emergency lakes: Hidden Hills and Cuddeback.
3. Flight duration: Approximately 11 minutes.
4. Flight plan based on 58,750lb thrust - Engine (#107).
Total burn time at 100% = 83 sec.
Launch Wt. = 33,200lb
Burnout Wt. = 15,550lb
2. FCS malfunctions as indicated on Analyzer check list.
3. Ball Nose, Inertial
Platform or APU Gear Box malfunction.
Failure | Action | ||
1. | Radio or Radar | Proceed as planned. | |
2. | Total
damper any axis,
failure to fixed gain any axis (For roll failure turn yaw off) |
(a) | 0
- 35 sec.
Alternate Flight Plan. Proceed normally until t = 35 sec. At 35 sec. pushover to 2° a and extend speed brakes to 35°. Shutdown at 5200 fps and retract speed brakes after shutdown. Vector to high key (q » 400 psf). Peak altitude » 140,000 ft. |
(b) | Attitude | (b) | Use 6° a at 28 sec instead of 38° q, then proceed with alternate flight plan. |
(c) | Ball Nose | (c) | Same as alternate, except use » 0.1 g instead of 2° a. Heading vernier to "·Y." |
3. | Total
damper any axis,
failure to fixed gain any axis (For roll failure turn yaw off) |
(a) | 35
sec - S.D.
Pushover to 2° a and extend speed brakes when failure occurs. Shutdown at 5200 fps. Reenter at 20° a and 20° speed brakes. |
(b) | Attitude | (b) | Same as 3 (a). |
(c) | Ball Nose | (c) | Same as 3 (a) except use » 0.1 g instead of 2° a. Use q = 0 for reentry. |
4. | Total
damper any axis,
failure to fixed gain any axis (For roll failure turn yaw off) |
(a) | After
Shutdown
Proceed as planned, reenter at 20° a. |
(b) | Attitude | (b) | Proceed as planned. |
(c) | Ball Nose | (c) | Use q = 0° for reentry. |
5. | Delayed engine light | Proceed - shut down at 5200 fps. |
6. Inadvertent engine shutdown:
0 - 42 sec Delamar
42 - 44 sec
44 - 68 sec Hidden Hills (2555 fps)
68 - 72 sec Cuddeback (3900 fps)
72 - Up sec Edwards (4200 fps)