FLIGHT NO: 3-36-59 DATE OF REPORT: 11-4-64
PILOT: Milt Thompson DATE OF FLIGHT: 10-29 & 10-30-64
CARRIER AIRCRAFT: B-52 #008 LAUNCH LAKE: Hidden Hills
PURPOSE OF FLIGHT: Captive Flight: Landing Gear Door Modification Checkout after
Cold Soak Flight
Flight: Landing Gear Door Modification Checkout
Boundary Layer Noise
Shear Layer Checkout
Center Stick Controller Evaluation
I. Discussion of Previous Operations
B. The NAA modified gear cable tension-regulator was installed giving a hot compensation of 3-3/4 inches. Gear handle travel with this configuration, measured at 13-7/8 inches, was considered excessive by the pilots. The cable was therefore shortened by 1 inch giving a hot compensation of 2-3/4 inches (the interim compensation was 2-1/4 inches prior to this modification). The rerigging accompanying the modification discussed in II-A increased the handle travel 1/2 inches, providing a final handle travel of 13-3/8 inches.
C. McDonnell B-44 ablative material was installed on lower speed brakes, lower ventral, rub strip on F-27, patch on lox tank, and a small strip just forward of the RH windshield.
D. The large wave roughness panel (240-931107-11) in F-4 position and the reference panel (240-931107-3) in F-3 position were installed.
E. Heaters were installed on the APU controllers per NAA EO's.
F. The elevator cover seal started leaking and was replaced. The new seal adhesive was cured by heating at 120°F for 12 hours.
(2) Strain gages on scoop door hook.
(3) Uplock hook, roller position.
(4) Scoop door hook position (CPT).
B. T/C's were connected to roughness panels (item II-D).
B. Both APU's were removed and reinstalled to repair bearing temperature instrumentation.
C. No engine run was accomplished based on the successful operation during the last flight. APU runs were accomplished on September 20, 1964. A calibration of the BLN microphones was accomplished during the APU run on APU electrical power.
D. A heat test of the new scoop door configuration was accomplished on October 24, 1964. Two tests were accomplished, one being the next profile and the other, the hottest profile that the aircraft would see. The nose gear door scoop door was heated, the aircraft nose was not heated. The gear was released after each heating cycle at 200°F.
E. The landing gear force and travel to release the gear was measured with an unloaded initiator. All three gears were released at 8-1/2 inch travel and 35 1b handle pull. The pilot released the gear after mating and prior to flight with a live initiator. Gear drop was satisfactory.
F. The aircraft was mated on October 29, 1964 to check the rewired MH-96 umbilical. The release had also been modified on the MH-96 umbilical plug requiring a demating to check the release mechanism.
G. The aircraft was mated for flight on October 29, 1964 after accomplishing item IV-F.
B. Flight 3-36-59 was accomplished on October 30, 1964.
The fire warning light came on about 54 seconds after engine shutdown.
Post flight; investigation revealed no signs of overheating in the engine
compartment, but the fire detector loop showed typical signs of having
been hot. As a result the YLR-99 engine, fire detector loop, and fire detector
relay will be changed prior to the next flight
Perry V. Row Vincent N. Capasso
X-15 Senior Project Engineer X-15 Project Engineer