FLIGHT NO: 3-24-41 DATE OF REPORT: January 13, 1964
PILOT: Milt Thompson DATE OF FLIGHT: November 27, 1963
CARRIER AIRCRAFT: B-52 #008 LAUNCH LAKE: Hidden Hills
PURPOSE OF FLIGHT: Pilot Checkout
I. Discussion of Previous Operations
B. Manometers measuring the wing static pressures and the upper ventral rakes were operational.
C. Several ball nose installations were made before an acceptable system was obtained:
Date Ball Nose S/N Remarks
11/12 002 Removed for hydraulic seepage and 20 cycle b oscillation
11/13 003 70° static port capped
11/14 004 Replaced S/N 003 which was suspected of pitot pressure leakage
12/14 004 Removed to adjust pitot pressure
Q/D, the cause of pitot system leakage
Ball nose S/N 004 was subsequently qualified for flight.
B. Flight 3-A-40 was aborted on 11/19/63 due to weather conditions at the launch lake.
C. H202 leakage from the #1 APU compartment drain was noted after captive flight. The pressure differential switch was leaking externally, and replacement of the switch was accomplished.
D. The flight scheduled for 11/20/63 was canceled by rain. Wet lake conditions delayed reschedule of the flight until 11/26/63.
E. The aircraft remained mated and was held in a preflight condition until the flight was accomplished.
B. Leakage of the engine #1 and #2 helium source was again noted during final system topoff procedures. Notable leakage was traced to inaccessible areas, and the flight was continued since rates were within acceptable limits.
C. The internal temperatures of the inertial system computer approached an overheat condition during the captive portion of the flight. Reference part I-A.
D. The pilot reported
sticky operation of the center stick mic button.
Perry V. Row Ronald S. Waite
X-15 Senior Project Engineer X-15 Project Engineer