FLIGHT NO: 3-19-30 DATE OF REPORT: June 25, 1963
PILOT: Maj. Rushworth DATE OF FLIGHT: June 18, 1963
CARRIER AIRCRAFT: B-52 #008 LAUNCH LAKE: Delamar
PURPOSE OF FLIGHT: Altitude Buildup
Vertical Tail Pressure Distribution Investigation
U. V. Experiment
I. Discussion of Previous Operations
B. Check valves and air oil separator installed on the APU gear case pressurization system to eliminate oil contamination to gear case pressure regulators and heat & vent system.
C. Miscellaneous brackets installed on elevator to support VCO's needed for heart pulse and blood pressure instrumentation.
B. Engine vibration pickup installed and checked out on internal tape recorder.
C. VCO sub-chassis enlarged for additional VCO's on blood pressure and heart pulse.
D. Landing gear drag brace instrumented with strain gages to obtain landing skid drag.
B. A successful engine run was performed on 6/8/63. This run was necessitated due to engine removal for installing the main landing gear oleo's.
C. A post flight investigation showed that #1 APU S/N 20 upper turbine seal was faulty and resulted in loss of gear case oil. This unit was replaced with APU S/N 17.
D. During the ground run for the APU's on 6/8/63, unstable vibration levels were observed on the #2 APU S/N 26. These runs were repeated on 6/10/63. Observation of the vibration levels revealed that after a short period of APU time, as the unit warmed up, the vibration level dropped. This instability was therefore blamed on a loose pickup and thermal shifts in the unit. Unit was accepted for flight.
E. After mating and during close-out of hydraulic servicing, a malfunction occurred in the hydraulic service stand which caused a pressure surge on the #l return system. This resulted in a rupture of a seal on the #l APU pump. Because of this, the airplane was demated to allow removal of the APU for a pump change.
F. During APU runs after reinstalling APU S/N 17, this APU lost a turbine bucket. The APU was removed and APU S/N 16, from X-15-1, was installed.
B. The stable platform malfunctioned prior to drop. This malfunction resulted in the loss of inertial altitude and vertical velocity and the pilot was required to use other means of estimating altitude throughout the high altitude portion of the flight.
C. During flight approximately 6" of the .008~ Inconel sheet over the crack in panel F-13 came loose. This portion was stitch-welded again after flight.
D. At engine shutdown a transient was experienced in sideslip.
Analysis showed that the engine was out of alignment to the left approximately
1/2 inch. Investigation on the airplane showed that in reality, it was
out 1/8 inch to the left. The alignment was moved 3/16 inch to the right
and final alignment with engine jigs was 1/16 inch to the right.
Perry V. Row John G. McTigue
X-15 Senior Project Engineer X-15 Project Engineer