Post-Flight: 2-47-84
DATE: August 3,
1966
PILOT: Maj. W. Knight
Everything went along
real well up through the checklist, except sometime on the way out the
inertial system had 100 feet/second rate of climb. Of course, this was
showing up on the velocity and I kept checking with Jack Russell on it
and we finally got it back to zero and then it went minus 100 feet/second
and the altitude went clear on down to 1200 feet/second. About this time
I had already aborted. (?) 12,000 feet, it went to. (?) Did I say 1200?
No, it went down to 12,000 feet/second. About this time, as I say, I had
already aborted, and that's why we got behind in the checklist a little
bit because I really wasn't too concerned with it. I figured any minute
Bill was going to call up and say, well, the inertial system was out of
spec; but everybody kept pressing on and I said OK, I'll catch up. We got
through the SAS check, I picked the time up there, and then we got a little
bit behind again. I still wasn't convinced at the four minute point. Getting
the jettison check, and I'd like to ask a question here on the jettison
check. Somebody had already said, at one time, that you have to have the
jettison into jettison for a long enough period to get the valves open.
I knew that I was going to be short on fuel, and I went to jettison and
back to pressurize about as fast as I could go, and Chase #1 called a good
jettison check on both of them. I would like to know where this valve time
comes in, because boy if you can do it any quicker, I'd like to know how.
I don't think that there is that much of a delay in those valves, that
you are talking about, because I did it about as fast as I could do it
and it was probably much less than a second, in jettison. (?) But we do
get a jettison check. OK. All right, we did get the jettison check and
went on in there. One other thing we missed back here on the BCS, and I
don't know why. This is the second time I've done that. The BCS check I
don't get the data on. Nobody called it, nobody caught it, no nothing,
but as soon as I was all through the BCS check, went down to turn the data
off and it wasn't even on. Well, I don't know why I missed that, but that
is the second time I have not turned the data on for the BCS check. The
launch was real good, The call for heading change was pretty obvious. I
had looked at the Startracker instrument and I knew I was off heading.
I had already started the correction and the call that Bill made, to correct
5° right, for track correction was real good. We caught that and made
it up, I think, before we ever got on theta. We made that correction there,
and between that correction and running out of trim, and we did run out
of trim at about Mach 2. I was real conscious of that, trying to get more,
and the alpha dropped off to about 10 and that's all I could get out of
it with full trim in. It did come up on theta, and I don't know why I had
so much trouble holding theta today other than the beta offset considerably
earlier than I had anticipated. It came in at about 3. I had probably a
half degree to a degree of beta offset at 3, whereas, in the simulator
it doesn't come in until about 4. I started correcting the beta and by
the time we got 47 or 48, I had almost full rudder in to try to correct
the beta and I still didn't have that zeroed. At that time, I noticed that
the theta was off again and Bill called for a theta correction. We got
it back on theta a little bit, but then trying to get the theta back and
holding the roll, the theta went to hell. It was probably off a degree
or maybe even more. No, much more than a degree at that time. I had almost
full rudder in trying to hold that thrust misalignment. We got up to the
shutdown and Bill called "standby for shutdown." It was real good, I had
a real good eye on the velocity and as it came up to 5000 I started back
on the throttle and I never did get the throttle all the way off before
it quit. It actually shut down before I got the throttle off. The time
on the clock was 81 3/4 seconds. Almost exactly what the simulator said.
After that, I got right on the BCS and got the beta lined up and the delta
psi on, and then went to zero alpha. I did not get it to zero alpha as
quick as I thought I would. I went down to zero alpha and a little bit
negative. I can't reach the experiment and test with my right hand, as
I was doing in the simulator. I sure can't do it, so I had to get it all
lined up. Then as the needles were lined up, I called "experiment on,"
I think. Did you get the call? )Yes I did) (?) Yes, it was, but I still
had not gotten down to the theta that I wanted, to get the needles lined
up. As soon as I got everything lined up, then I called the experiment
on and I was going through about 250,000 on the inertial altitude. So when
your call came in that I was going high it wasn't really a surprise. I
was a little bit concerned about the reentry then, because I didn't know
whether you were correct or the inertial system was correct and I thought
if it were 238, it was going to be a rough one. We got the experiment on
and the tracking was probably within one or two units all the way around,
on the tracking. We should have gotten that with no problem. (?) Yes, it
was all lined up, I engaged it, the light came on and things jumped to
zero and we had it right there. It was a long 42 seconds before the light
went out. I wasn't really worried about anything until that light went
out. I think somebody called "experiment off" and the light had gone off
about 3 or 4 seconds before that. Then I reached over and turned the experiment
off manually, after the light went out, and it also had been trimming in,
the trim on the side stick, but I had not gotten it to full trim yet. Then
I turned the RAS off and about that time the alpha started down, and Bill
came back and asked me to get the alpha back up. I think if I had had the
full trim in it would have been a little bit better. That's what I had
planned to do. The other thing was that, on the top, when I made corrections
with beta, roll and pitch, each time the needles would jump. I was getting
interference with the BCS system and the ball nose. They would really jump.
I think that the needle, on the beta, went left most of the time. I can't
really coordinate between the needle position and what control I was using,
because the minute I saw it I knew what it was and then I kind of discarded
it and said, well, (You should not have seen that on your beta needle.)
Well, it jumped a couple of times. I am sure that beta needle jumped. We
will look at the film. (?) No, I don't think so. I think when I hit the
BCS a couple times the beta needle jumped. We will look at that on the
cockpit film. Coming back in, people began to get concerned about the beta
and the alpha, and I could see what was happening. I didn't have the full
trim to hold it. I went off RAS, and when I turned the RAS off, then the
alpha started down; but I had something else to do right then and it probably
went clear down to 7 - 8°. I knew it was there and I knew I had a little
time to get it back up, and then Bill started hollering about the alpha.
So we got it back up and it went back up about some 20 - 21 or 22°.
(25) OK. I knew it was up there, but again I was not worried about it because
we still were not back down to any q. So I got the alpha settled down and
the beta squared away. As the reentry came on and the q started to pick
up we got just a little bit of beta oscillation, probably a half degree
or a degree at the most, of beta. That steadied out, I had good alpha,
I had full trim in, and I held the full trim and I got up to about 5 g
and the q went to about 1400 and no higher, on my indication. As soon as
the q stopped I went back and I looked at the h dot, and the h dot was
coming through about 400. I backed off and we stopped it at about
200 to 100 feet per second. and then had to really push over to get it
started back downhill with the full brakes. The q never went over 1400
throughout the entry nor on the way down. From then on somebody asked if
I had the field in sight. I did not have the field in sight. I had not
even worried about looking at it yet. The next thing that was of significant
value was that Bill called something like 50 or 60,000 feet and I was still
showing about 80 or 90,000 feet on the inertial. So, I went to the pressure,
at that time, and I was down to 50. Then I rolled it and looked for the
field and could see the field then. I rolled it back out and headed out
towards California City. That's why I was concerned about getting altitude
checks from Jerry, Chase #4, because the inertial system had gone kaput.
It was still way up 60, 70,000 as I came down through 30 or 35. The pattern
from then on worked out real well, I crossed the field about 30, probably
a little higher. Turned and landed about 2/10 of a mile short of the smoke.
It should have been a real good touchdown and probably about 5500 feet
rollout, push and pull. All extend was pulled at about, oh, Mach 2, and
whatever altitude it was when it turned. I did not see anything on the
pressure system, nothing at all. Everything worked good all the way down
from there. I don't think I had time to look at the outer trim. It did
not feel like it was, once we had shut down. Of course, on the way up when
I had almost full rudder in I had a lot of aileron in too trying to hold
it. It seemed to be almost the opposite of what the simulator showed, in
the fact that I did need almost full rudder. I did not need nearly as much
aileron as I thought I was going to need to hold the roll and the beta.
I probably did not get the beta within two degrees of center, but I did
come off of everything at shutdown. I didn't get too many transients in
there at all. (?) No, I did not. Reentry was very smooth and I thought
it was a very good reentry in that we held everything until it all steadied
out. (?) No, I used full trim and you may find a little bit of force on
the stick, but I don't think very much at all. I knew I was high and
I knew it was going to be a higher q reentry than I had anticipated, but
I don't think I pulled in that much. I don't think I can tell you. I was
concentrating very strongly on making sure that I held that alpha until
the h dot came up to a reasonable figure. I did feel the doors open and
shut. Being as it was the first time, I can't tell you which condition
it was, but I thought that there was a little bit of a pitching
motion with the doors either coming open or going closed. I can't remember
which one, Jim, but I did feel them. I did not see the light. I heard the
doors and then looked and the light was on. My max altitude, on inertial,
was 258. The inertial was bad, on the way down, and when I stopped on the
lakebed I called out the readings on the inertial system, and I still had
some pretty good altitude and some pretty healthy h dot. I don't remember
what it is now. I think it was about 800 feet/second climb in h dot. I
forget what the altitude was now. (?) Everything came back in before drop
and we were reading 45,000, 44 and about zero h dot and about 800 feet/second,
and it all looked good. Then Jack said the platform is in spec, we went.
That was a comment I was going to make to you, Butch. After last night,
you wanted to abort four o'clock. Visibility was good everywhere and even
coming back in. I heard the calls all the way down and knew pretty well
where I was. But when you called "did I have the field in sight," I didn't.
I had not even started looking for the field yet. I knew I had plenty of
altitude and you kept calling on track so I knew I was pretty close to
right on. Then, after I got everything all squared away and got my head
back up out of the cockpit, then I rolled it left and looked down and right
there was the field and it was right on. Everything worked good except
the inertial altitude and that, I wanted to get some good correlation between
my pressure altitude and what Jerry was reading. We seemed to be a little
bit off, on the higher altitude. As we came down to 25 and 30, then we
were pretty close. Before, either I misread it or something, but there
was quite a difference in what he was calling and what I was showing on
my pressure altitude. On the way back down, once I got the q on and I felt
some acceleration, then I knew that things were coming along; so I dropped
off the BCS and I can't tell which was the last BCS input. Pitch, roll
or yaw. (?) I don't think so. No. I did not feel anything like that. No,
I didn't. I would say that if we could get the engine aligned, to get the
beta out of there, that it would help. Although it did not cause as much
of a problem as I thought it would. When I came off of everything there
were no real large transients at burnout as I came off of all controls.
It just kind of stayed there, I had about 10 or 15° left roll and about
2° needle right on the beta. As I came off it, it kind of all stayed
there. So it really wasn't a big transient and it did not seem to be a
real large problem. I don't know what you would get if you left your feet
on the floor and let it go out there 4 or 5° beta and then shut down.
I don't know. This is the way we had talked about doing it, and that is
what I did and it seemed to work out real well. I think next time we should
be able to zero the beta and zero the roll; knowing now what kind of control
displacement that is required to do it. Yes, I would say it was pretty
close to full rudder and I was still out on beta. (?) Yes. There was some
beta oscillations right at the beginning on the way down, but nothing more
than about 1/2° and it wasn't bad at all. I was kind of set for the
reentry because I really did not know whether I was at 257 or 247.