FLIGHT NO: 2-37-64 DATE OF REPORT: May 14, 1965
PILOT: John B. McKay DATE OF FLIGHT: April 28, 1965
CARRIER AIRCRAFT: B-52 #008 LAUNCH LAKE: Hidden Hills
ENGINE: S/N 110
PURPOSE OF FLIGHT: (1) Stability & Control Data
(2) Thermal Loading Effects on Landing Gear
(3) Star Tracker Functional Checkout
(4) Landing Dynamics
I. Discussion of Previous Operations
B. Investigation of the RH main gear uplock system failure (reported in the last report for flight 2-36-63) supports the theory that excessive loading of the main uplock hook is caused by thermally induced bowing of the main strut. Ground heating tests made to simulate aerodynamic heating of the main-gear struts for a calculated "hot flight" profile (2-22-40) caused bending of the hook and release of the gear (complete description of these tests and results are contained in separate reports from the Structural Mechanics Section, FRC.)
As a result of these tests the main-gear uplock has been
modified to include:
2. Belleville washer mounting system to provide approximately .14 inch "bowing" of the strut (as measured at the uplock roller).
3. Increased strength of back-up structure on bulkhead.
B. Modified differential pulley for landing gear actuating cable system to improve cable alignment.
C. Marotta solenoid valve installed to "lock in" emergency jettison source pressure to permit pilot to maintain tanks in jettison mode down through landing.
D. Incorporated the following EO's to provide additional "hot compensation" in the speed brake system:
878856
878855
E. Incorporated the following miscellaneous EO's:
894466
882590
898262
892602
882445
F. Installed bushing in LH horizontal stabilizer actuator trunnion fitting (salvage for oversize hole.)
G. Installed appropriate instrumentation to record:
2. Belleville washer compression (LH & RH)
3. Hook vs uplock roller position (RH only)
4. Various main gear strut skin temperatures (LH & RH)
5. Strut bowing (RH only)
B. On Saturday 2/6/65, extensive salvage repair of buckled RH fuselage longeron was started (see discussion under item I B.)
C. On Tuesday, 3/30/65, a heat test with modified main uplock hook design (Belleville washers) was conducted. No permanent deformations or failures were noted. The test was deemed successful and the uplock system was approved for flight test.
D. On Thursday, 4/8/65, the engine ground run was completed. Heavy rain followed and resulted in enforced "down" time for all X-15 aircraft.
E. On Thursday, 4/23/65, the APU ground run was completed.
B. Flight squawks resulting from this flight were:
1. Unprogrammed roll oscillations.
2. Inertial altitude failure.
3. Startracker system failed to meet test objectives largely
due to inadequate switch controls. A modified pilot control system will
be incorporated for the next flight
Perry V. Row William P. Albrecht
X-15 Senior Project Engineer X-15 Project Engineer