Flight No.: 2-22-40 Scheduled Date : May 4, 1962
Pilot: Major Robert Rushworth
Subject of Test : Heat transfer, ASAS checkout and high angle of attack stability with partial speed brakes.
Airplane Configuration: Basic X-15
Launch: Hidden Hills
on magnetic heading of 218°. ASAS "Armed."
No. | Time | Alt | V | a | Event |
1. | 0 | 45 | 790 | 0 | Launch, light engine, increase to 100% T, rotate until 2g is attained. |
2. | 25 | 49 | 1800 | 10 | Maintain 2g until q = 20°, maintain q = 20°. |
3. | 39 | 54 | 2500 | 4 | Pushover to 0 g. |
4. | 70 | 73 | 4600 | 0 | Reduce to 30% T, increase a to maintain 1 g (a » 3°). |
5. | 75 | 73 | 5000 | 3 | Modulate speed brakes to maintain 5000 fps (dj » 25° deflection). |
6. | 103 | 73 | 5000 | 3 | Burnout. |
7. | 115 | 73 | 4600 | 3 | Roll to 60° right bank and increase a until 5g is attained or to dh = -25, perform dv step input. |
8. | 130 | 73 | 4000 | - | Roll to 0° bank angle, extend maximum speed brakes, decrease a to 5°. |
9. | 150 | 71 | 3000 | - | Disengage roll SAS, perform dv step input. |
10. | 160 | 70 | 2400 | - | Reengage SAS, perform dv step input. |
12. Check ventral armed, pressurize tanks.
13. Before APU shutdown,
cycle controls, retract flaps, set stabilizer trim to zero, and push-to-test
ball nose. Data off.
2. q vernier will be set at 20°, a crosspointer will null at 0°.
3. Emergency Lakes: Three Sisters and Cuddeback.
2. Malfunction of inertial platform attitudes.
3. Malfunction of ball nose.
2. If ball nose fails, proceed as planned.
3. If total pitch or roll SAS fails, proceed as planned, do not exceed 8°a.
4. For inadvertent engine shutdown; prior to 39 seconds, return to Hidden Hills, 39 to 50 seconds proceed to Three Sisters, 50 to 65 seconds proceed to Cuddeback, above 65 seconds proceed to Edwards - two engine restarts may be attempted in all cases.
9. If cabin pressure is lost proceed with alternate flight plan.