Date: April 28, 1967
Pilot: Maj. M. Adams
For me the checklist
went real good today. I never got behind at all. We could have if we'd
worried about the radio which did not work too well from approximately,
I think it was ten minutes down to about two minutes. In between I had
a little trouble receiving, but I had a lot of chase support relaying and
nothing sounded wrong, so I pressed on and it all worked out real well.
We got down to the launch, dropped away with the engine, got a good light
and rotated. I should mention that just before launch I looked up at the
precision heading and roll, and again they were looking erratic. They were
jumping maybe one to two units, both of them, and they looked noisy and
when I see something noisy I hate to rely on it. Then during the rotation
they still looked noisy, like they were not precise indications, so I flew
mostly the eight ball to control my heading and my bank angle. When I got
the call to make a slight correction, I didn't really correct it on the
ball, I just turned to the right a little bit and rolled it back out and
pressed on, and it looked like it worked out pretty good. I was keeping
track of the time on theta and theta started coming down - it was approaching
20 some seconds so then I started concentrating on the vernier and then
it looked like I had another problem come up. The theta vernier seemed
to be overly sensitive. I could never get it in the center, and when I
put in a small correction to correct toward it, it would jump to the other
side and I started to chase it all around so finally I just more or less
flew about five a
and put in little inputs towards it once in a while to try to center it.
So I think there is something wrong either with the setting and the sensitivity
or just the sensitivity itself, because I could not control theta. I had
the same problem on the last flight evidently. I just thought, in the last
flight I did not do such a good job but now I just think that compared
to the simulator and what I saw in the first flight, that there is something
wrong with the sensitivity of theta. (?) Well I never really switched,
I cross checked to see that I was holding the right a
there to hold that q,
but if I had the wrong q
holding that a
would still be wrong. I did have about 5 or 6 a
somewhere in there. So I think the q
vernier would bear watching. I also looked at the precision heading and
roll, during the boost, for the rotation and it was still noisy so I gave
up on that and I just went to the eight ball like I said before. In the
burn while I was trying to hold q
I checked b
and it looked like I did have a little thrust misalignment. I'd say that
I might have had about maybe 1° of nose left to contend with, and I'd
take it out part of the time and I guess it was building with velocity
and it started to slip back in, and I kept trying to correct it as we went
along. There was a little problem, I think, with the inertial velocity
readout. I noticed a little glitch in the turn, it jumped around maybe
50 feet per second. From about nine it would jump up to 950 fall back to
nine. We rolled out on the launch heading it was down around 600 and it
stayed fairly stable after that. But then during acceleration during the
boost, it seemed to be sticking and erratic. I would not expect the rate
of increase to be linear but it should show a constant increasing trend
and it was not doing that. It was speeding up and then it would slow down
and then it would jump again, and as it got near to 4600 I noticed it,
up around 48 it made one final fast swoop up towards 5000. The time was
looking about right so I shut down when it hit 5200, but the clock showed
83 seconds. An extra long burn time, and I think I got a little more overshoot
than you normally get, so I think the inertial velocity might bear looking
into. So due to my control or the q
vernier or something, we got - we never went high enough. I was getting
Jack's calls real good and I had made up my mind when I saw us peaking
out, I had about 164, I wasn't going to extend the experiment, and he said
not to and we didn't. Going over the top flying the eight ball I kept q
about equal to zero on the eight ball and got up to about 20°. I could
feel the onset of g during the reentry, and saw the H dot decreasing and
I anticipated or I think I over.......... a little bit, because I started
to level off and then I saw, well it was still down around 800, and it
seemed to be holding there and so I came back in with some and I ended
up holding 15 a
for the rest of the reentry. Then when I was satisfied that it had re-entered,
about 600, I pushed over and put out the speed brakes and started coming
home. For some reason I heard, about in between 50 miles from Cuddeback,
I could hear some kind of noise, sounded something like the BCS out there
firing. I thought maybe I had, for some reason, had the RAS on then, and
I looked down, the switches were off. It was kind of a swooshing noise,
periodically. Then I turned off the BCS to see if that would help and it
still seemed to be making that noise, so I turned the BCS on, forgot about
the noise. I don't know when it went away. It seemed to have the right
energies. It came over the high key. I got the call to put the speed brakes
in a little early, which I didn't want to do, but it was a good call because
I ended out over the high key with 40,000 and at about Mach one. Then in
the pattern the only time I really felt like saying anything, which wasn't
important anyway, I noticed that the transmitter had a lot it sounded like
garbled back ground tones, so I don't think the radio then was transmitting
in the aircraft very well. Used speed brakes in the pattern quite a bit.
Probably left them out a little bit too long because I was a little bit
short of energy at my aiming point out there. Got all the switches, flared,
flaps, gear, and touchdown, and that is about all I have to say about the
flight. Oh, I heard just one little thump. I don't know what it was. It
just was a very very small thump going out, so I thought as long as Colonel
Sorlie was out there, might as well take a look and see if it was something
external. He didn't find anything and I never heard it but that one time
so it didn't turn out to be anything. It was a very minor thump. (?) No.
I did not seem to have any trim difficulties. I held my 10 a
in the rotation instead of 11 as I was told to do. It seems like I over
rotated and I never quite got back there, but I don't think I had less
than 10, and it seemed like I had plenty of authority this time. (?) No.
During the boost there was no trim roll to contend with.