FLIGHT NO: 1-66-111 DATE OF REPORT: 8/17/66
PILOT: John B. McKay DATE OF FLIGHT: 8/11/66
CARRIER AIRCRAFT: B-52 #003 LAUNCH LAKE: Delamar
ENGINE SERIAL: 107 APU #1 16AN APU #2 20AN
PURPOSE OF FLIGHT: 1. Apollo Horizon Scanner
2. Wing Pods(a) Micrometeorite
(b) Skybrightness
(c) Pace Transducer
(d) RH Pod Vibration
3. Electrical Loads
I. Discussion of Previous Operations
B. The "C" band
radar failed for the two previous flights because of a blown fuse. Between-flight
checks of the circuitry and the radar components failed to reveal the cause.
Prior to this flight, a grounding of the "C" band radar switch with an
adjacent switch was located; normal operation was obtained for this flight.
B. A fit check of
the PMR experiment was accomplished on 8/2/66. Both upper and lower elevators
were installed, the flip-top lid was installed, and the experiment was
manually extracted to verify the possibility of installation. Interferences
noted included:
2. Contact between the experiment extending pneumatic source bottle and actuator pneumatics lines, to be corrected by line relocation.
3. Contact between experiment mirror support post (forward LH side and the tie-angle for the forward door hinge pivot) to be corrected by redesign of the tie-angle.
4. Contact of the
upper elevator post closeout cover and the lower elevator cutout, to be
corrected by enlarging the cutout hole. The post also contacted the oscillograph
drum mounted on the bottom of the lower elevator which can be cleared with
a 45° 1/4 inch chamfer of the post container.
C. The IFDS effort
between Flight 1-65-108 and 1-66-111 is listed as follows:
2. The vertical velocity indicator, instrument digital converter, and the computer were removed for laboratory checks. No problems were noted during runs. The computer components which are related to the vertical velocity indication function were replaced.
3. Another IFDS computer, vertical velocity indicator, and computer were installed and operated in the aircraft on 8/5/66. A combined run with SAS, MIT was later completed without malfunction.
4. The IFDS computer memory was lost during a power transient on Flight l-A-109 with precision B-52 power at 13 minutes to launch.
5. The IFDS computer used on the previous flight (with new vertical velocity circuit cards) was installed on 8/9/66 after Flight l-A-109. The system was preflighted before servicing on the morning of 8/10/66.
6. IFDS operation was demonstrated with APU power transfer on Flight l-A-110 without malfunction.
7. The power system
voltage transients were again experienced in Flight 1-66-111 with computer
dump and loss of data accuracy. See item I, A.
2. One protective panel because of a sticky relay.
3. No. 1 AC bus voltage regulator (it was intended to replace the No. 2 bus regulator; however, markings were in error) in relation to the IFDS power problem.
4. Elevator lid
seal was cut during the PMR experiment fit check.
F. The aircraft was mated to B-53 #003 on 8/8/66.
G. Flight l-A-109 was completed on 8/9/66 with J. B. McKay as pilot. The IFDS computer memory was lost during a B-52 precision power transient. The IFDS computer was replaced. Post-flight cleanup revealed a leak in the No. 2 APU tank bladder which was replaced. The pitch-yaw RAS valve was replaced because of inflight leakage. The manual BCS roll-valve was also replaced when malfunction occurred during the pitch-yaw valve checkout. This effort extended into the start of propellant service the following morning.
H. Flight l-A-110 was completed on 8/10/66 with J. B. McKay as pilot. Several delays were incurred with the IFDS preflight checkout. The flight was canceled at the initial outbound course because of launch lake helicopter malfunction. The IFDS was demonstrated with an APU start and a power transfer from B-52 precision power to the APU bus. A ball-nose problem was suspected; however, post-flight checkout did not show a problem and good operation was obtained during the Flight 1-66-111.
B. The electrical power system transients with corresponding tripout of SAS, and IFDS dump was again obtained as described in part I, A.
C. A flight dynamic-pressure level of 2050 psf was experienced during the reentry. No apparent fuselage or horizontal stabilizer distortions or distress were noted during a quick inspection following flight.
D. The aircraft
swung sharply to the left after landing. The landing gear shock-strut service
was suspected as a contributing cause; however, the horizontal stabilizers
were held full nose-down with little roll input available for direction
control. A 15-knot side component also was affecting aircraft rollout.
Perry V. Row Ronald S. Waite
X-15 Senior Project Engineer X-15 Project Engineer