FLIGHT NO: 1-61-101 DATE OF REPORT: 11/10/65
PILOT: Capt. J. Engle DATE OF FLIGHT: 10/14/65
CARRIER AIRCRAFT: B-52 #003 LAUNCH LAKE: Delamar
ENGINE SERIAL: 108 APU #1 16 APU #2 20
PURPOSE OF FLIGHT: 1. MIT Horizon Photometer (Phase I)
2. Pace Transducer (LH Pod Nose)
I. Discussion of Previous Operations
B. The MIT Horizon Scanner, Phase I with tailcone box were installed as the prime experiment.
C. The air density Pace transducer was installed in the LH wing pod nose cone.
B. APU runs accomplished on 10/2/65 were satisfactory. A RAS leak check indicated leakage from the pitch up rocket motor however, cycling the valve eliminated a major portion of the leakage. This valve caused the flight abort (l-A-100). The RAS valve could not be operated in the airborne configuration as it is on the ground. An in-flight RAS test switch is proposed to allow airborne valve operation.
C. An extended closed canopy cockpit and regulator purge was accomplished the day before flight l-A-100.
D. Flight l-A-100 was accomplished on 10/8/65, intended as a flight demonstration for the X-15 conference. Capt. J. Engle was pilot and the aircraft was mated to B-52 #003. The abort was caused by excessive leakage from the RAS pitch up rocket. A spurious IFDS malfunction detector signal was obtained on the first attempt to operate the IFDS on the ground before flight; the indicated computer gross malfunction did not represent actual system operation and was accepted for flight. Restart of the system eliminated the indicator malfunction. The abort flight data was removed from the two oscillographs and the tape recorder in order to evaluate the MIT temperature environment. Adjustments were made in the MIT experiment compartment temperature sensors to raise the temperature level as result of the data evaluation.
E. The RAS pitch-yaw valve was replaced after l-A-100. Engine preflight functionals and IFDS computer reload was accomplished Monday, 10/11/65.
F. The flight was canceled after pilot entry on 10/13/65 because of weather.
B. The cabin helium source pressure leakage was excessive with launch accomplished at 2250 psig; 900 psig remained after landing.
C. The SAS yaw channel disengaged at launch and was reset by the pilot. The yaw again disengaged during reentry when severe yaw oscillations were encountered. Reset could not be accomplished until the oscillations were damped out.
D. Consumption of APU H202 was sufficient to require use
of the H2O2 transfer system.
Perry V. Row Ronald S. Waite
X-15 Senior Project Engineer X-15 Project Engineer