Flight No.: 1-55-89 Scheduled Date : June 8, 1965
Pilot: Milton O. Thompson
Purpose : To obtain data for the following programs:
2. Honeywell Inertial System Checkout (George Krueger)
3. Cross Track Vernier (George Krueger)
Instrumentation Engineer - (Don Yount)
Launch Point Coordinates:
37° 18' N, 114° 36' W
No. | Time | Alt | Vel | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine, increase to 100% T. Rotate at 10° a ( » 2g) until q = 30°. |
2. | 27 | 50 | 1850 | 10 | 663 | q = 30°. Maintain q = 30°. |
3. | 40 | 60 | 2400 | 5 | 663 | Pushover to zero g. |
4. | 49 | 70 | 2900 | 0 | 500 | Extend speed brakes to 35°. |
5. | 81.5 | 97 | 5150 | 0 | 506 | Shutdown, retract speed brakes. |
6. | 99 | 104 | 4900 | 0 | 342 | Peakaltitude - increase a to maintain Hdot = -200 fps. |
7. | Cuddeback - Vector to High Key. Speed brakes as required. Engine Master "OFF." | |||||
8. | High Key - check flap and "Squat" circuit breakers in. | |||||
9. | Before APU shutdown, cycle flaps, set stabilizer trim to zero, data "OFF." |
NOTES:
2. Emergency Lakes: Hidden Hills and Cuddeback.
3. Flight Duration: Approximately 11 minutes.
4. Flight plan based on 57,250# thrust engine.
Total burn time at 100% = 86 sec.
Launch wt. = 33,000#, Burnout wt. = 14,950#, 300# allowed for in-flight jettison.
2. Malfunction of any SAS channel.
3. Malfunction of inertial platform.
4. Total Ball Nose failure.
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1. | Radio or Radar | Proceed as planned. | ||
2. | Total Pitch Damper | Maintain a > 0°, proceed as planned. | ||
3. | Total Yaw Damper | Proceed as planned except pushover to 2° a at 53,000 ft. instead of zero g. | ||
4. | Total Roll Damper | Same as 3 except turn Yaw Damper off. | ||
5 | Attitude Failure | Use 5° a in place of 30° q. | ||
6. | Ball Nose | Proceed as planned. | ||
7. | Delayed engine light | Pushover to zero g at H = 53,000 ft. (Hdot » 1000 fps). | ||
6. | Inadvertent
engine shutdown:
00 - 47 sec. Delamar 47 - 71 sec. Hidden Hills (2700 fps) 71 - 77 sec. Cuddeback (4200 fps) 77 - Up Edwards (4600 fps) |