Flight No.: 1-47-74 Scheduled Date : April 28, 1964
Pilot: Major R. Rushworth
Purpose of Flight: Phase II Optical Degradation Experiment and checkout of Optical Attitude Indicator.
Launch: Delamar Lake #1 on magnetic heading 214°, SAS Hi-Lo-Hi (8-4-8), ASAS "ARMED", both BCS "OFF", RAS "OFF," heading vernier to "Standby," Ventral OFF.
Launch Point Coordinates:
37° 18' N, 114° 36' W
No. | Time | Alt | Vel | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine, increase to 100% T. Rotate at 11° a until q = 30°. Heading vernier to "·y." |
2. | 22 | 49 | 1600 | 11 | 480 | q = 30°. Maintain q = 30°. |
3. | 38 | 60 | 2300 | 5 | 600 | Pushover to 0 g. (Hdot » 1000 fps.) |
4. | 71 | 89 | 4500 | 0 | 550 | Extend speed brakes to 20°. |
5. | 84 | 97 | 5700 | 0 | 600 | Shutdown at 5700 fps. |
6. | 91 | 100 | 5600 | 0 | 500 | Increase a to » 5°. (q» 5°). Maintain a» 5° to peak altitude. |
7. | 105 | 102 | 5500 | 4 | 440 | Nellis - Peak altitude - Maintain q and f within ±8°. (Manual A). Descend at 200 ft/sec to 70,000 ft. |
8. | 145 | 97 | 5050 | 4 | 470 | Pahrump - Maintain q and f within ±8°. (Manual B). |
9. | 148 | 96 | 5000 | 4 | 480 | Retract speed brakes. |
10. | 248 | 73 | 3500 | 4 | 750 | Pilot Knob - Maintain q and f within ±8°. (Manual C). |
11 | 263 | 70 | 3300 | 4 | 760 | 70,000 ft - Maintain 70,000 ft. |
12. | 293 | 70 | 3000 | 4 | 640 | Cuddeback - Maintain q and f within ±8°. (Manual C). Vector to High Key. Speed brakes as required. Engine Master "OFF." |
13. | High key - Check flap and "Squat" circuit breakers in. | |||||
14. | Before APU shutdown, cycle flaps, set stabilizer trim to zero, data "OFF." |
NOTES:
2. Emergency Lakes: Hidden Hills and Cuddeback.
3. Flight Duration: Approximately 11 minutes.
4. Flight plan based on 58,500# thrust engine.
Total burn time at 100% = 86 sec.
Launch wt. = 33,500#, Burnout wt. = 15,300#.
5. Manual V/H settings:
A = .055
B = .051
C = .047
D = .043
2. Malfunction of any SAS channel.
3. Malfunction of inertial platform attitudes.
4. Total Ball Nose failure.
5. APU gearbox pressurization malfunction.
6. "Test" malfunction.
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1. | Radio or Radar | Proceed as planned. | ||
2. | Total Pitch Damper | Maintain a > 0°, proceed as planned. | ||
3. | Total Yaw Damper | Proceed as planned except pushover to 2° a at 52,000 ft instead of zero g. Heading vernier to "Standby." | ||
4. | Total Roll Damper | Same as 3 except turn Yaw Damper off. | ||
5. | Attitude | Use 5° a in place of 30° q. | ||
6. | Ball Nose | Proceed as planned. | ||
7. | Delayed engine light | Pushover to zero g at H = 55,000 ft (Hdot » 1000 fps.) | ||
8. | Inadvertent
engine shutdown:
00 - 46 sec. Delamar Lake 46 - 67 sec. Hidden Hills (2700 fps) 67 - 72 sec. Cuddeback (4200 fps) 72 - Up Edwards (4600 fps) |