Flight No.: 1-42-66 Scheduled Date : Dec. 3, 1963
Pilot: Major R.
Rushworth
Purpose of Flight:
Phase II Optical Degradation experiment and ·
cross range indicator checkout.
Launch: Delamar
Lake on magnetic heading 214°, SAS Hi-Lo-Hi (8-4-8), ASAS "ARMED",
both BCS "OFF", RAS "OFF". Heading vernier to "·y."
Ventral OFF.
Launch Point Coordinates:
37° 18' N, 114° 36' W
No. | Time | Alt | Vel | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine, increase to 100% T. Rotate to 2 g. |
2. | 15 | 45 | 1500 | 11 | 500 | 2 g - maintain 2 g until q = 30°. |
3. | 25 | 48 | 1800 | 10 | 650 | q = 30°. Maintain q = 30°. |
4. | 35 | 58 | 2300 | 5 | 660 | Pushover to 0 g. (Hdot » 950 fps). |
5. | 66 | 88 | 4500 | 0 | 580 | Extend speed brakes to 20°. |
6. | 78 | 97 | 5700 | 0 | 600 | Shutdown at 5700 fps. |
7. | 93 | 103 | 5550 | 0 | 430 | Increase a to » 5°. (q» 5°). Maintain a» 5° to peak altitude. |
8. | 103 | 104 | 5450 | 5 | 400 | Nellis - Peak altitude - (Maintain q and f within ±8°). Descend at 200 ft/sec to 70,000 ft. |
9. | 140 | 97 | 5050 | 4 | 460 | Pahrump - (Maintain q and f within ±8°). |
10. | 142 | 96 | 5000 | 4 | 480 | Retract speed brakes. |
11 | 245 | 70 | 3500 | 4 | 880 | 70,000 ft. - maintain 70,000 ft. |
12. | 253 | 70 | 3350 | 4 | 800 | Pilot Knob - (Maintain q and f within ±8°). |
13. | 290 | 70 | 2800 | 4 | 560 | Cuddeback - (Maintain q and f within ±8°). Test Mode to "Landing" (q > 0°). Pushover to a» 2°, vector to High Key. Speed brakes as required. Engine Master "OFF." |
14. | High key - Check flap and "Squat" circuit breakers in. | |||||
15. | Before APU shutdown, cycle flaps, set stabilizer trim to zero, data "OFF." |
NOTES:
2. Emergency Lakes: Hidden Hills and Cuddeback.
3. Flight Duration: Approximately 11 minutes.
4. Flight plan based on 60,000# thrust engine.
Total burn time at 100% = 78.5 sec.
Launch wt. = 32,800#, Burnout wt. = 15,000#.
2. Malfunction of any SAS channel.
3. Malfunction of inertial platform.
4. Total Ball Nose failure.
5. APU gearbox pressurization malfunction.
6. "Test" malfunction.
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1. | Radio or Radar | Proceed as planned. | ||
2. | Total Pitch Damper | Maintain a > 0°, proceed as planned. | ||
3. | Total Yaw Damper | Proceed as planned except pushover to 2° a at 55,000 ft. instead of zero g. Heading vernier to "Standby." | ||
4. | Total Roll Damper | Same as 3 except turn Yaw Damper off. | ||
5. | Attitude Failure | Use 5° a in place of 30° q. | ||
6. | Ball Nose | Proceed as planned. | ||
7. | Delayed engine light | Pushover to zero g at Hdot = 950 fps. | ||
8. | Inadvertent
engine shutdown:
00 - 42 sec. Delamar 42 - 62 sec. Hidden Hills (2700 fps) 62 - 67 sec. Cuddeback (4200 fps) 67 - Up Edwards (4600 fps) |