FLIGHT NO: 1-40-64 DATE OF REPORT: 11/20/63
PILOT: M.O. Thompson DATE OF FLIGHT: 10/29/63
CARRIER AIRCRAFT: B-52 #008 LAUNCH LAKE: Hidden Hills
PURPOSE OF FLIGHT: 1. Pilot Checkout 2. Optical Degradation Experiment
Demonstration
I. Discussion of Previous Operations
B. The ART 15A mount did not uncage during the previous flight due to loss of 115V AC power. A broken connection at the elevator disconnect was the cause.
B. The K5-25 experiment cooling ring was removed to prevent the possibility of temperature gradients in the experiment structure.
B. The experiment operation mode switch was modified to replace the previous three-position switch with a two-position variety.
C. Provisions for recording the ART 15A mount axis vibrations were completed.
B. Three lox tank regulator installations were made before an acceptable component was obtained. Two regulators were replaced, one for higher than normal source unlock pressure and the second for external leakage. The original regulator was removed to support X-15-3.
C. Rain on October 16, 1963 required flight reschedule and a repeat of the aircraft preflight.
B. The side-stick trim knob friction was inadequate, requiring continuing pilot attention.
C. The delta-cross-range pilot's display was inoperative.
Review of preflight adjustments and procedures revealed the system null
point was wrong, causing the apparent malfunction.
Perry V. Row Ronald S. Waite
Senior X-15 Project Engineer X-15 Project Engineer