Flight No.: 1-40-64 (Alternate) Scheduled Date : Oct. 18, 1963
Pilot: Milton O. Thompson
Purpose of Flight: Pilot checkout, · cross range indicator checkout.
Launch: Hidden Hills on magnetic heading 212°, SAS Hi-Lo-Hi (8-4-8), ASAS "ARMED", both BCS "OFF", RAS "OFF". Heading vernier to "Standby." Ventral off.
Launch Point Coordinates:
36° 20' N, 115° 59' W
No. | Time | Alt | Vel | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine at 75%T, decrease to 50% T, maintain 50% T. Rotate at 10° a until q = 20°. |
2. | 26 | 46 | 1200 | 10 | 310 | q = 20°, maintain q = 20°. |
3. | 69 | 65 | 2300 | 5 | 475 | Pushover to zero g. |
4. | 83 | 72 | 2800 | 0 | 500 | Extend speed brakes to 35°. |
5. | 90 | 74 | 3100 | 0 | 570 | Increase a to maintain Hdot = 0. |
6. | 122 | 74 | 4000 | 4 | 940 | Shutdown (shutdown will be accomplished at 4000 ft/sec or 128 sec whichever occurs first). Retract speed brakes. Maintain H » 74,000'. |
7. | 130 | 74 | 3700 | 4 | 800 | Perform moderate right and left rolls and rudder pulses. Vector to Pilot Knob. |
8. | 185 | 74 | 2950 | 4 | 500 | Pilot Knob. |
9. | 200 | 74 | 2800 | 4 | 460 | Descend at » 400 ft/sec. Vector to High Key. |
10. | 220 | 62 | 2500 | 3 | 650 | Cuddeback, continue to High Key (Hdot » -400 ft/sec). Engine Master "OFF." |
11 | High key - Check flap and "Squat" circuit breakers in. | |||||
12. | Before APU shutdown, cycle flaps, set stabilizer trim to zero, data off. |
NOTES:
2. Emergency lake: Three Sisters and Cuddeback.
3. Flight Duration: Approximately 9 minutes.
4. Flight plan based on 56,000# thrust engine (35,200# for 50%).
Total burn time at 50% = 133 sec.
Launch wt. = 32,800#, Burnout wt. = 15,000#.
2. Malfunction of any SAS channel.
3. Malfunction of inertial platform.
4. Malfunction of Ball Nose.
5. APU gearbox pressurization malfunction.
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1. | Radio or Radar | Proceed as planned. | ||
2. | Total Pitch Damper | Proceed as planned. | ||
3. | Total Yaw Damper | Proceed as planned except pushover to 2° a at 69 sec. instead of 0 g. Do not perform roll and rudder pulse maneuvers. | ||
4. | Total Roll Damper | Same as 3 except turn Yaw Damper "OFF.". | ||
5. | Attitude Failure | Use 5° a in place of 20° q at 26 sec. | ||
6. | Ball Nose | Proceed as planned. Use 1.5g at 10 sec. instead of 10° a for rotation. | ||
7. | Delayed engine light | Pushover to zero g at H = 65,000 ft (Hdot = 600 fps). | ||
8. | Inadvertent
engine shutdown:
00 - 72 sec. Hidden Hills 72 - 78 sec. Three Sisters (2400 fps) 78 - 95 sec. Cuddeback (2600 fps) 95 - Up Edwards (3200 fps) |