FLIGHT NO: 1-39-63 DATE OF REPORT: 11/5/63
PILOT: Capt. J. Engle DATE OF FLIGHT: 10/7/63
CARRIER AIRCRAFT: B-52 #008 LAUNCH LAKE: Hidden Hills
PURPOSE OF FLIGHT: 1. Pilot Checkout 2. Optical Degradation Experiment
Functional Demonstration
I. Discussion of Previous Operations
B. Further analysis of the engine malfunction which occurred after the throttle shutdown of the previous flight indicated actuation of the lube oil low pressure switch produced the malfunction. Pressure variations in the lube oil system under near zero "G" condition are suspected.
B. Main landing gear struts incorporating the beefed-up design were installed because of deterioration of strut attachment hole diameters. Other parts of this design were not included since parts were not available.
C. Emerson Electric Thermolag 500 was applied to the leading edge and side panels of the lower stub ventral and to each lower speed-brake surface.
D. As part of the fuselage window boundary-layer rake installation, the communications antenna was relocated to the C. G bay lower access door (previous lower bug-eye camera location).
E. The mixing-chamber pneumatic control-gas converter capacity was increased by reinstalling the tubing coils around the blower motors. The temperature of the gas is now considered satisfactory for extended mixing-chamber operation.
F. The lower ventral actuator and related mechanism were removed to reduce weight.
B. A display of delta cross-range using inertial system outputs was provided in the cockpit center pedestal to assist in course correction for the KS-25 experiment.
C. The pilot's blood pressure system was installed.
D. Provisions for recording the output of the Air Force high temperature alpha-vane were incorporated.
B. The left hand inner windshield was replaced due to surface scratches.
C. A successful engine run was accomplished on August 21, 1963.
D. APU S/N 25AN was reinstalled in the #l position following test stand requalification. The APU was removed at a later date for use in X-15-3 due to lack of spare units. APU S/N 25AN was returned again and installed.
E. The KS-25 experiment encountered a shutter failure requiring the shutter assembly to be sent to Fairchild for repair. The unit was rapidly returned, which allowed closeout and mating on Tuesday, September 4, 1963.
F. Rain occurred on September 4, 1963, canceling the proposed flight and the aircraft was demated.
G. Preflights were reinitiated following the rain, however, rains on September 17, 1963 again delayed flight preparations. Preflights were reinitiated on September 23, 1963.
H. Flight l-A-62 was accomplished on October 4, 1963. The flight was canceled due to complete failure of the X-l5 communications system. A loose coaxial connection and inadequate power-supply antenna connector engagement were located and corrected.
B. The angle-of-attack indicator malfunction recurred after launch and the indicator remained inoperative throughout flight.
C. Hydrogen Peroxide was observed leaking from the LN2 compartment area after flight. The leak was traced to the upper flange of the #1 APU tank and attributed to permanent set of the RTV88 material which acts as a sealing gasket at this point.
D. The LH electrical umbilical disconnect removed with
the X-15 at launch. Separation occurred at the soldered connections at
the back of the plug. This disconnect assembly did not incorporate a strengthened
lanyard attach point, and failure to disconnect was due to separation of
the metal eye. The replacement disconnect incorporated the revised pin
design.
Perry V. Row Ronald S. Waite
Senior X-15 Project Engineer X-15 Project Engineer