Flight No.: 1-37-59 Scheduled Date : July 2, 1963
Pilot: Joseph A. Walker
Purpose of Flight: Optical Degradation experiment, RAS Checkout, and Traversing probe development
Launch: Delamar Lake on magnetic heading 214°, SAS 8-4-8, ASAS Armed, both BCS "ON", RAS "OFF", Ventral off.
Launch Point Coordinates:
37° 18' N, 114° 36' W
No. | Time | Alt | Vel | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine, increase to 100% T. Rotate to 2g. |
2. | 12 | 45 | 1300 | 11 | 420 | 2g - maintain 2g until q = 33°. |
3. | 24 | 49 | 1700 | 10 | 510 | q = 33°, maintain q = 33°. |
4. | 81 | 131 | 5200 | 6 | 120 | Shutdown. Maintain » 6° a. Engage RAS, Auto cutoff "ON." |
5. | 105 | 180 | 4900 | 6 | 16 | Pushover to zero a. Maintain zero a until q = 0°. ·y switch to "·y." |
6. | 134 | 210 | 4700 | 0 | 9 | q = +8°, maintain q and f within ±8° to Cuddeback area. |
7. | 154 | 220 | 4600 | 0 | 6 | Peak altitude. Extend speed brakes to 20°. Maintain q ª 0° until a = 20°. ·y switch to standby at » 180,000 ft. |
8. | 213 | 165 | 4950 | 20 | 30 | a = 20°. Maintain 20° a until 4 g. |
9. | 250 | 87 | 4500 | 20 | 550 | 4 g - Maintain 4 g until Hdot = -500 fps (Max reentry q » 630). |
10. | 253 | 84 | 4300 | 18 | 600 | Hdot = -500 fps, pushover to a» 3°, extend speed brakes to 35°, check RAS "OFF." Engine master "OFF." |
11. | 285 | 67 | 3300 | 3 | 900 | Cuddeback - pull up to q > 0°. Test mode to "Landing", push over to a» 3°. |
12. | 316 | 56 | 2100 | 3 | 630 | Retract speed brakes (if energy permits), push over to a = 0° for » 3 sec. Vector to High Key. Speed Brakes as required. |
13. | High key - Check flap and "SQUAT" circuit breakers in. | |||||
14. | Before APU shutdown, cycle flaps, set stabilizer trim to zero, data off. |
NOTES:
2. Emergency lake: Hidden Hills and Cuddeback.
3. Flight Duration: Approximately 10 minutes.
4. Flight plan based on 57,000# (100%) and 36,800# (50%) thrust engine. Total burn time at 100% = 83 sec. Launch wt. = 32,800#, burnout wt. = 15,000#.
2. Malfunction of inertial platform attitudes.
3. Malfunction of ball nose.
4. APU gearbox pressurization malfunction.
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1. | Radio or Radar | Proceed as planned. | ||
2. | Total
Pitch Damper
Total Roll Damper (Turn Yaw off) |
(a) | 0
- 40 sec.
Pushover to .2 g at 40 sec. and reduce to 50% T at 50 sec., shutdown at 5000 fps and extend S.B. to 20°. Retract S.B. at 4500 fps. Hmax » 135,000 ft). Maintain a > 0°. |
|
(b) | 40
sec. to S.D.
Pushover to .2 g and reduce to 50% T when failure occurs, shutdown at 5000 fps and extend S.B. to 20°. Retract S.B. if reentry is required. Maintain a > 0°. |
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(c) | After
S.D.
Use » 15° a for reentry (» 1000 q reentry). |
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3. | Total Yaw Damper | Proceed as Planned. Maintain a > 0°. | ||
4. | Attitudes | (a) | 0
- 40 sec.
Use 5° a at 24 sec. instead of 33° q, then proceed with 2(a). |
|
(b) | 40
sec - S.D.
Same as 2(b). |
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5. | Ball Nose | (a) | 0
- 40 sec.
Same as 2(a). |
|
(b) | 40
sec. - S.D.
Same as 2(b). Use q = 0° for reentry. |
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6. | Delayed engine light | Proceed - shutdown at 5200 fps. | ||
7. | Inadvertent
engine shutdown:
00 - 46 sec. Delamar 46 - 65 sec. Hidden Hills (2700 fps) 65 - 70 sec. Cuddeback (3900 fps) 70 - Up Edwards (4300 fps) |