FLIGHT NO: 1-34-55 DATE OF REPORT: 5/6/63
PILOT: J. B. McKay DATE OF FLIGHT: 4/25/63
CARRIER AIRCRAFT: B-52 #008 LAUNCH LAKE: Delamar
PURPOSE OF FLIGHT: Induced Turbulence with KC-1
I. Discussion of Previous Operations
B. Both APU's, S/N 16AN and S/N 26AN, were removed from the aircraft following the previous flight to inspect the pinion gears for wear. APU S/N 16AN was reinstalled in #l position, and S/N 26AN was installed in X-15-3 for flight 3-14-24. APU S/N 26AN was removed from X-15-3, an APU Test Stand Run accomplished to survey the vibration signature, and reinstalled in the #2 position in X-15-1.
C. The engine S/N 107 was qualified for flight without a ground run based on post flight inspection and flight data records.
D. Propellants were serviced and a prime check was accomplished to demonstrate the replaced fuel shutoff valve and the lox pump bearing probe operation. Eight minutes of precool-prime with tanks pressurized produced a lox pump bearing temperature indication of -18°F.
E. The MLG struts were inspected visually and all welds were dye-checked.
F. The flight was canceled on April 25, 1963 because of uprange weather following complete propellant service.
B. Mixing chamber temperature on the #l system regulated at -20°C. Platform cooling was adequate.
C. The engine operated until propellant depletion. Lox depletion occurred in spite of fuel off-loading with 17 gal. ullage.
D. The KC-1 landing mode was engaged at a point approaching
high key with the pilot executing a slow pitch, roll maneuver. The gimbal
locks did engage, however, a weight compensating system continued to operate
and jammed as it drove against its stop. A circuit change will be incorporated
to deactivate the weight shifter with landing mode selection.
Perry V. Row Ronald S. Waite
X-15 Senior Project Engineer X-15 Project Engineer