Flight No.: 1-31-52 Scheduled Date : 7/16/62
Pilot: J. A. Walker
Subject of Test: Investigation of: 1. Notch filter at high dynamic pressure 2. Stability in ASAS mode 3. Aerodynamic drag.
Launch: Mud Lake
on magnetic heading 177°, ASAS armed, SAS 6-10-8.
No. | Time | Alt | V | a | q | Event |
1. | 0 | 45 | 790 | 2 | 145 | Launch, light engine - increase to 100% T, rotate to and maintain 6° a to q = 30°, maintain q = 30°. |
2. | 32 | 45 | 2200 | 6 | 1220 | Maximum q. |
3. | 45 | 65 | 2800 | 2 | 1020 | Pushover to 0 g. |
4. | 80 | 100 | 5400 | 0 | 440 | Shut down - set SAS 6-6-0 (yar off) - perform dv pulse. |
5. | 142 | 105 | 5200 | 0 | 290 | Pullup to 5° a. Perform da pulse. |
6. | 151 | 95 | 5100 | 5 | 480 | Pullup to 10° a - perform da pulse. |
7. | 166 | 78 | 4800 | 10 | 840 | Pullup to a » 15° - perform da pulse. |
8. | 182 | 82 | 4000 | »15 | 625 | Pushover to 0 "g." |
9. | 205 | 85 | 3800 | 0 | 420 | Extend speed brakes. |
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10. | 236 | 65 | 3100 | 0 | 900 | Retract speed brakes - perform pullup, pushover maneuver (a = 0 - 10 - 0). |
11. | 262 | 50 | 2400 | 0 | 1100 | Perform pullup - pushover maneuver (a = 0 = 10 = 0), vector to high key. |
12. | 287 | 50 | 1600 | 0 | 480 | Perform pullup, pushover maneuver (a = 0 - 10 - 0). Jettison (H2O2 off). |
13. | High key - check, ventral armed, pressurize tanks, push-to-test ball nose, perform pushover-pullup maneuver (a » 8, 0, 8). |
Notes:
2. q vernier will be set at 30°, a crosspointer will null at 6°.
3. Emergency lakes, Grapevine and Cuddeback
2. Malfunction of inertial platform attitudes
3. Malfunction of ball nose
4. Malfunction of radio, radar or microwave
2. If radio or radar fail proceed as planned .
3. For inadvertent engine shutdown:
Prior to 45 sec, return to Mud Lake
45 - 65 sec, Grapevine
65 - 70 sec, Cuddeback
Greater than 70 sec, Rogers
Two engine starts may be attempted
4. For yaw damper failure do not increase a above 15°.
5. For total pitch or roll damper do not increase a above 12°.
6. For ball nose failure, proceed through burnout, fly 1 "g" after burnout.
7. For delayed engine light pullup at 2-1/2g..